Gj. Brauckmann et al., EXPERIMENTAL AND COMPUTATIONAL ANALYSIS OF SHUTTLE ORBITER HYPERSONICTRIM ANOMALY, Journal of spacecraft and rockets, 32(5), 1995, pp. 758-764
During the high-Mach-number, high-altitude portion of the first entry
of the Shuttle Orbiter, the vehicle exhibited a nose-up pitching momen
t relative to preflight prediction of approximately Delta C-m = 0.03.
This trim anomaly has been postulated to be due to compressibility, vi
scous, and/or real-gas (lowered specific heat ratio gamma) effects on
basic body pitching moment, body-flap effectiveness, or both. In order
to assess the relative contribution of each of these effects, an expe
rimental study was undertaken to examine the effects of Mach number, R
eynolds number, and ratio of specific heats. Complementary computation
al solutions were obtained for wind-tunnel and flight conditions. The
primary cause of the anomaly was determined to be lower pressures on t
he aft windward surface of the Orbiter than deduced from hypersonic wi
nd-tunnel tests with ideal- or near-ideal-gas test flow The lower pres
sure levels are a result of the lowering of the flowfield gamma due to
high-temperature effects. This phenomenon was accurately simulated in
a hypersonic wind tunnel using a heavy gas, which provided a lower ga
mma, and was correctly predicted by Navier-Stokes computations using n
onequilibrium chemistry.