S. Kurum et al., PLANT OPTIMIZATION BY RETROFITTING USING A HIERARCHICAL METHOD - ENTRAINER SELECTION, RECYCLING AND HEAT INTEGRATION, Journal of chemical technology and biotechnology, 70(1), 1997, pp. 29-44
Systematic procedures for reducing wastes in complex chemical plants a
re needed to allow efficient optimisation. Here, a hierarchical proced
ure was applied to the optimisation of a real industrial plant to redu
ce wastes as well as energy and raw material consumption. In the case
studied, the continuous production of methyl-butynol (MBI), acetylene
reacts with acetone. The solvent ammonia and acetylene are recycled to
the reactor. Unreacted substrates and by-products are separated from
the product stream by distillation. Part of the unreacted acetone can
be reused for other purposes after distillation. A substantial part of
the unreacted substrates and by-products is delivered to a wastewater
treatment plant. These waste streams constitute a substantial problem
for the operation of this plant. First, waste streams were characteri
sed and tracked back to their origin. Following the hierarchical desig
n procedure, the overall input-output structure was fixed. The entrain
er in the present process was critically examined and options were sug
gested. Then various recycle schemes were considered for later detaile
d study. The existing plant was simulated using ASPENPLUS. After adjus
ting the model to all important aspects of the real process scheme, ex
cellent agreement between actual process performance data and simulati
on was obtained. The various process schemes were simulated and assess
ed for their economic and ecological performance. The objective functi
ons used included utility, substrate and catalyst costs, as well as co
sts for wastewater treatment. Additionally, the environmental burden r
elated to energy supply was accounted for by a carbon dioxide tax as s
uggested by the Nordic countries. The process changes included separat
ion of unreacted acetone from the product stream and recycling to the
reactor. By-products were converted back to substrates in an additiona
l reactor separation system and recycled. In various simulated process
configurations and operational schemes substantial economic and ecolo
gic improvements were achieved. This study demonstrates the usefulness
of hierarchical approaches combined with process simulation for plant
optimisation.